DSpace at VNU: Effects of Hydraulic Retention Time on Organic and Nitrogen Removal in a Sponge-Membrane Bioreactor

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DSpace at VNU: Effects of Hydraulic Retention Time on Organic and Nitrogen Removal in a Sponge-Membrane Bioreactor

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ENVIRONMENTAL ENGINEERING SCIENCE Volume 30, Number 4, 2013 ª Mary Ann Liebert, Inc DOI: 10.1089/ees.2012.0385 Effects of Hydraulic Retention Time on Organic and Nitrogen Removal in a Sponge-Membrane Bioreactor Bui Xuan Thanh,1,* Ha˚kan Berg,2 Le Nguyen Tuyet Nguyen,1 and Chau Thi Da Faculty of Environment, Ho Chi Minh City University of Technology, Ho Chi Minh City, Vietnam Swedish International Biodiversity Program (SwedBio), Stockholm Resilience Center, Stockholm University, Stockholm, Sweden Faculty of Agriculture, An Giang University, Long Xuyen City, Vietnam Received: September 27, 2012 Accepted in revised form: January 1, 2013 Abstract This is the first study on application of a sponge-membrane bioreactor (sponge MBR) for recirculation of aquaculture wastewater in the Mekong delta, Vietnam Performance of a sponge MBR with a moving-cube sponge medium (20% v/v) was evaluated at different hydraulic retention times (HRTs) for the specific example of catfish pond wastewater The sponge MBR was operated at HRT values of 8, 4, and h, which correspond to membrane fluxes of 5, 10, and 20 L/m2 per hour, respectively The average chemical oxygen demand (COD) removal efficiencies were maintained at 93%, 94%, and 87% at an HRT of 8, 4, and h, respectively, while the average total nitrogen (TN) removal efficiencies were 84%, 70%, and 57% The COD and TN removal efficiencies decreased with a decrease in HRT (increase in membrane flux) Permeate concentrations of COD and TN were as low as 6.3 and 2.7 mg/L at the operated HRTs, respectively Compared to the conventional MBR, the sponge MBR had twice the TN removal capacity at the same HRT due to simultaneous nitrification–denitrification In addition, results implicated that the fouling rate (dTMP/dt) increased in an inverse proportion with HRT (h) according to the power equation (fouling rate = 4.2474 HRT - 2.225) Free movement of sponges in the reactor improved fouling due to sweeping of the cake layer on the membrane surface Results reveal that the sponge MBR was effective in terms of simultaneous organic and nitrogen removal, fouling control, and water recirculation Key words: catfish farm; fouling rate; hydraulic retention time (HRT); nitrogen removal; sponge-membrane bioreactor (sponge MBR); wastewater Introduction I n recent years, aquaculture production has increased rapidly, mainly due to increasing catfish production in the Mekong delta provinces in southern Vietnam This development generates profit and income, but it also bears the risks of a negative environmental impact such as pollution or biodiversity change (Anh et al., 2010; Konnerup et al., 2011) Catfish production requires a large amount of fish feed, in the form of wet homemade feed, trash fish, and pellets These feeds are partly transformed into fish biomass and partly released into the water as suspended solids or dissolved matters such as organic carbon, nitrogen, and phosphorus These wastes originate from surplus food, feces, and excretions via the gills and kidneys Other pollutants are the residuals of drugs used to cure or prevent diseases Unless the wastewater of catfish *Corresponding author: Faculty of Environment, Ho Chi Minh City University of Technology (HCMUT), Vietnam Building B9, 268 Ly Thuong Kiet St., District 10, Ho Chi Minh City 70000, Vietnam Tel/ Fax: + 84.8.3.863.9682; E-mail: bxthanh@hcmut.edu.vn ponds is treated before it is discharged directly into rivers, it adversely impacts the receiving waters with increased risks for eutrophication and declining water quality This may have a direct negative effect on the catfish production itself, but also on other water users relying on good water quality Aquaculture development and management should take into account the full range of ecosystem functions and services, and should not threaten the sustained delivery of these services to the society at large (Soto et al., 2008) Therefore, the selection of a catfish wastewater treatment process for reuse and recycling is necessary in sustainable catfish farming Biological removal of organic compounds and nutrients from polluted aquaculture wastewater is an appropriate process for water quality and water reuse The common biological methods include activated sludge process, biofilter, aerated lagoon, and constructed wetlands However, these approaches often demand a large area due to the requirement for a high hydraulic retention time (HRT) Some treatment processes also have to be operated during a limited time after harvesting fish, when the treated wastewater is discharged into the river In these situations, a compact and efficient 194 SPONGE-MEMBRANE BIOREACTOR TREATING CATFISH FARM WASTEWATER membrane bioreactor (MBR) is proposed to be the most appropriate wastewater treatment solution The MBR combines the aerobic degradation with a direct solid–liquid separation of activated sludge using a microfiltration or ultrafiltration membrane MBR provides better performance than conventional activated sludge, including a smaller required area, higher quality of treated wastewater, and long sludge retention time Further, high biomass retention in the MBR makes it able to operate at high loading rates, with a comparable small reactor volume The filtration process can remove microorganisms without chemical disinfection (Visvanathan et al., 2000) Moreover, the use of a medium in the MBR could improve MBR operation, which may increase the treatment performance by high biomass concentrations and reduced membrane fouling (Leiknes and Ødegaard, 2001; Thanh et al., 2012) The presence of the moving medium in the membrane tank can also reduce fouling The mechanism reducing of the fouling membrane can cause the moving medium in the MBR tank capable of enhancing the combination of suspended and colloidal particles on the surface of the medium for reducing fouling and clogging on the membrane surface Jamal Khan et al (2011) studied the performance of the MBR process in combination with a sponge medium at an HRT of h (representing 15% volume reaction tank) to remove chemical oxygen demand (COD), total nitrogen (TN), and total phosphorus (TP) Results show that the effective removal of COD, TN, and TP with the sponge MBR is 98%, 89%, and 58% This is higher than the standard MBR, which had a removal of 98%, 74%, and 38% for COD, TN, and TP, respectively Guo et al (2008b) found that the sponge MBR (sponge occupies 10% of reactor volume) results in a twofold enhancement of the filtration flux of the MBR This clearly shows that the addition of sponges to MBR can reduce the contamination loading of the MBR Sponge has been considered as a suitable medium because it can act as a mobile carrier for active biomass, resulting in improved organic and nutrients removal, as well as reduce membrane fouling (Chae et al., 2004; Ngo et al., 2006; Guo et al., 2009) In addition, thick biofilm that is formed on the surface of the sponge is regularly removed by friction of individual sponge cubes with each other, whereas the fixed microorganisms within the sponge are very stable and active (Chae et al., 2004) Sombatsompop et al (2006) investigated the effect of the HRT on membrane performance and sludge properties MBRs were operated at different HRTs of 2, 4, 6, and h The MBRs consisted of three bioreactors that included suspended growth without a medium, a moving medium, and a fixed medium The removal efficiency of COD in the moving medium was found to be 98% with a short HRT of h The nitrogen removal was accomplished by microorganism assimilation and nitrification reaction in the MBR at all HRT values This study aims to investigate the effect of different HRTs on treatment performance and fouling of sponge MBR for catfish wastewater treatment and recirculation Table Parameter pH COD NH4+ -N NO2- -N NO3- -N TP Composition of Wastewater Used Unit Value Mean (min–max) — mg/L mg/L mg/L mg/L mg/L 7.35 66 10 0.65 0.25 1.69 (6.9–7.8) (22–167) (2–24) (0–3.5) (0–2) (0–4) The real catfish farm wastewater was used at the beginning of the study From day 88 onward, similar synthetic wastewater component was substituted due to serious natural flooding that occurred in the study area COD, chemical oxygen demand; TP, total phosphorus end of the 4-h HRT), serious flooding occurred in the provinces that inundated the pond Thus, synthetic wastewater was replaced for catfish farm wastewater The synthetic wastewater was made of catfish pellets with addition of NH4Cl The concentrations of COD, NH4+ -N, NO2- -N, NO3- -N, and TP were similar to those of the real catfish pond wastewater (Table 1) MBR and operating conditions The MBR has a working volume of 40 L with a submerged hollow-fiber membrane module (Tianjin Motimo Membrane Technology, Tianjin, China; surface area of m2, nominal pore size of 0.2 lm) The MBR was operated in a cyclic condition (8 on/2 off) The sponge MBR was operated at HRTs of 8, 4, and h The solid retention time was controlled at 30 days for all HRTs (Table 2) Dissolved oxygen was maintained at a level higher than mg/L by stone diffusers The transmembrane pressure (TMP) was recorded daily by a pressure gauge When the TMP reached a set-point value of 40 kPa (membrane fouling), a backwash pump (Blue-White Industries, Huntington Beach, CA) was automatically operated to flush off the caked layer formed on the membrane surface The flow rate of the backwash pump was set at 20 L/h for However, in this study, the backwash only occurred at the highest HRT of h Before the system started a new run, the membrane was cleaned by chemicals (0.5% NaOH and 0.5% NaOCl) for h Seed sludge for the sponge MBR was taken from a conventional activated sludge process (70% v/v) and sediment from the bottom of a catfish pond (30% v/v) The initial mixed liquor suspended solids (MLSS) concentration was approximately of 6000 mg/L Sponge medium Polyurethane sponge, with a density of 18.2 kg/m3, and a sponge cube of cm · cm · cm were used as a moving Table Operational Periods of Sponge Membrane Bioreactor Materials and Methods Parameter Wastewater Permeate flow (L/day) Flux (L/m2 per hour) HRT (h) Wastewater was collected from a catfish farm located in Long Xuyen City, An Giang province, Mekong delta, Vietnam In the later stage of the experiment (after day 88, at the 195 Period Period Period 120 240 10 480 20 HRT, hydraulic retention time 196 THANH ET AL medium The sponges were added in the MBR proportional to 20% of the reactor volume (Guo et al., 2010) Analytical methods Analyzed parameters were COD, nitrite, nitrate, ammonia, TP, MLSS, and mixed liquor volatile suspended solids (MLVSS) The biomass concentration in the sponges was estimated according to Guo et al (2010) Analytical methods were done according to the standard methods (APHA, 1998) Nitrogen balance was estimated by Equation (1): TNin ẳ TNout ỵ TNassimilated ỵ TNdenitrification ð1Þ Nitrogen assimilated into the cell biomass was estimated based on the produced volatile-suspended solids (VSS) The assimilated nitrogen was equal to 12% VSS (Metcalf & Eddy, Inc., 2003) The nitrogen balance was conducted to estimate the simultaneous nitrification–denitrification (SND) that occurred in the sponge medium All results were statistically compared by one-way analysis of variance using Minitab 16 Results and Discussion COD removal The average COD removal efficiency during the operating period is shown in Table The removal efficiency of COD ranges between 87% and 94% with an HRT ranging from to h The average COD concentrations in the permeate were *6.3 mg/L for the operated HRTs A similar observation was reported by Coˆte´ et al (1997), who suggested the effluent COD from a hollow-fiber MBR was maintained at a level below 16 mg/L, despite a five-stage change in the HRT from to 24 h, and Guo et al (2008b) found the COD removal efficiency over 97% The COD removal was maintained at 93% and 94% at an HRT of and h, respectively, but was 87% at an HRT of h, which indicates that the HRT affects the permeate quality in terms of COD removal This is in contrast to the result of Sombatsompop (2006), who reported that the MBR provided an excellent and stable effluent quality at HRT values between and h The permeate COD not only complies with the Vietnam National Technical Regulation on the effluent of aquacultureprocessing industry, QCVN 11:2008/BTNMT (50 mg COD/ L), but also reaches the Vietnam National Technical Regulation for surface water quality, QCVN 08:2008/BTNMT (100 mg COD/L) Moreover, the organic content in treated wastewater was removed to a level that would make the water acceptable for such uses as park irrigation, vehicle washing, firewater, flushing a toilet, or aquaculture recirculation, according to the U.S Environmental Protection Agency (USEPA, 2004) Based on these guidelines, the treated wastewater can be recycled directly to the catfish pond Nitrogen removal Characteristics of catfish pond wastewater are mainly ammonia (NH3) with its derivatives, NH4+ -N, NO2- -N, and NO3- -N Ammonia and nitrite are harmful substances for aquatic animals In a catfish pond, ammonia is generated by the natural decomposition of proteins, which are residues from various sources including zooplankton, fish excrement, and uneaten food The average concentrations of NH4+ -N, NO2- -N, NO3- -N, and TN in catfish wastewater treated with the sponge MBR are summarized in Table During the operational period, the NH4+ -N removal efficiencies at HRTs of 8, 4, and h were 100%, 99%, and 86% in the sponge MBR, respectively, which implies slightly better nitrification at a higher HRT Guo et al (2009) reported ammonia nitrogen removal of > 99% with 10% sponge medium at an influent ammonia nitrogen concentration of 15–20 mg/L Jamal Khan et al (2011) mentioned NH4+ -N removal of 95.6% with 15% sponge medium at an HRT of h Liu et al (2010) reported that increasing HRT from to h could enhance the NH4+ -N removal from 47.2% to 98.1% Table indicates that there was no significant improvement between HRTs of h and h in terms of NH4+ -N elimination, as almost all (99%) had been removed after h The average nitrite concentration was *0.03 mg/L with HRTs of and h, but > 1.0 mg/L with an HRT of h This indicates a limited nitrification capacity of the MBR during a short retention time An HRT of h is too short to achieve complete nitrification This result is similar to the result of Sombatsompop (2006) The results infer that changes of HRT affect the nitrogen removal efficiency of the sponge MBR TN removal efficiencies of the sponge MBR were 84% – 8%, 70% – 18%, and 57% – 21% at HRTs of 8, 4, and h, respectively This indicates that TN removal of the sponge MBR increases with an increasing HRT In the sponges, nitrification probably takes place on the surface of the sponge, whereas anaerobic/anoxic conditions inside the sponge provide a suitable environment for denitrification (Nguyen et al., 2010) This phenomenon is SND A higher HRT enriches slowgrowing microorganisms and creates effective contacts between microorganisms and substrates SND occurs in the sponge medium because of the biomass captured within the pores of the sponge and a limited oxygen concentration inside Table Chemical Oxygen Demand Removal Performance in Sponge-Membrane Bioreactor COD concentration and removal efficiency at different HRTs Parameter COD in influent (mg/L) COD in permeate (mg/L) Removal efficiency (%) 8h 4h 2h QCVN 08:2008/BTNMT USEPA, 2004 48 – 14a – 3a 93 – 5a 78 – 23b – 2a 94 – 2a 83 – 38b 11 – 7b 87 – 7b — 10–50 — — 10 (BOD) — Data was analyzed by Minitab 16 Statistical Software abc Superscript letters denote significant differences among periods of operation Means in the same row that not share the same letter are significant different ( p < 0.05) SPONGE-MEMBRANE BIOREACTOR TREATING CATFISH FARM WASTEWATER Table 197 Concentrations of Nitrogen and Total Phosphorus in Wastewater Treated with the Sponge-Membrane Bioreactor Concentration in permeates (% removal efficiency) at different HRTs [mg/L (%)] Parameters NH4+ -N NO2- -N NO3- -N TN TP 8h 4h 2h QCVN 08:2008/BTNMT – 0a (100a) 0.03 – 0.05a 1.58 – 0.98a 1.61 – 1.01a (84 – 8a) 0.11 – 0.16a (82 – 26b) 0.13 – 0.32a (99 – 2a) 0.03 – 0.05a 2.70 – 1.44b 2.86 – 1.64ab (70 – 18b) 1.18 – 0.47b (56 – 8c) 1.45 – 1.83b (86 – 17b) 1.02 – 0.75b 1.21 – 0.99a 3.68 – 2.63b (57 – 21c) 0.31 – 0.29a (64 – 20c) 0.1–1 0.01–0.05 2–15 — 0.1–0.5 (PO4- ) TN = NH4+ -N + NO2- -N + NO3- -N Data was analyzed by Minitab 16 Statistical Software abc Superscript letters denote a significant differences among periods of operation Means in the same row that not share the same letter are significantly different ( p < 0.05) TN, total nitrogen the pores This explains the comparatively high TN removal in the sponge MBR (Yang et al., 2009) Therefore, an HRT of 4–8 h could be the appropriate operating time for nitrogen removal in this system Figure provides a simplified illustration of the possible mechanism for nitrogen removal through SND in the sponge MBR The nitrification reaction occurs nearly completely at HRTs of and h, as the concentrations of TN are low in the membrane permeate of the sponge MBR The TN concentration in the permeate at 2-h HRT is almost twofold higher than those at other HRTs These results indicate that the reaction time of 2-h HRT is not enough for SND to occurr in the sponge MBR The HRT influences the nitrogen removal capacity of the sponge MBR Fig also shows that the amount of TN denitrified at HRTs of and h in the sponge MBR is 72% and 62% higher than at HRTs of and h in a conventional MBR (no sponge in the MBR), where the amount of TN denitrified was 40% and 27% It is inferred that the sponge medium can achieve complete nitrogen removal through SND The percentage of denitrification in sponge MBR is twice that in a conventional MBR at the same HRT Table presents the average removal of TP in the sponge MBR, which is 82%, 56%, and 64% at HRTs of 8, 4, and h, respectively TP removal at a 4-h HRT is lower than that at a 2-h HRT probably because the concentration of TP in the influent at a 4-h HRT was lower than that at a 2-h HRT The TP removal efficiency in this study is 82% higher in comparison with a conventional MBR: 58% in the sponge MBR, and 38% in FIG Nitrogen balance in a sponge-membrane bioreactor (sponge MBR) the MBR without sponge in the studies of Jamal Khan et al (2011) Biomass in sponge MBR Figure shows that the biomass accumulated in the MBR with time from 8- to 4-h HRT The trend was similar for biomass in sponges The rate of biomass formation in sponges was higher than that in suspended growth; thus, the ratio of MLSS in sponge/total MLSS increased with the operation time, showing that the shorter the HRT, the higher the ratio More biomass in sponges enhanced more TN removal and fouling control It is observed that when operated at a 2-h HRT (high flux of 20 L/m2 per hour), the biomass started releasing from the sponges, and a large amount of biomass attached strongly to the membrane module This resulted in total biomass reduction in the reactor since day 138, and serious fouling occurred in the 2-h HRT operating period (as described in the Fouling propensity of sponge MBR section) The average total biomass in sponges and in suspension was 3908 – 813 mg/L during this stage The level sensor had a problem on day 148; the biomass was lost, and the total MLSS remained 2882 mg/L Then, the total MLSS started increasing and reached 5136 mg/L on day 158 The MLVSS/MLSS ratio ranged from 0.21 to 0.69 during operation The ratio reduced from 0.43 to 0.21 during the 8-h HRT This was due to the endogenous respiration in the sponge MBR (F/M = 0.07–0.52 mg COD/mg VSS per day) The ratio increased from 0.24 to 0.6 at 2- and 4-h HRTs The FIG Biomass fraction in the sponge MBR with time 198 THANH ET AL FIG Profile of transmembrane pressure (TMP) with time (left) and fouling rate (right) MLVSS/MLSS ratio in the sponge MBR was lower than that in a conventional MBR Fouling propensity of sponge MBR Figure shows the variation of the TMP during the operation of the sponge MBR The results show that TMP development fluctuated from 3.5 to kPa in 58 days, from to 18 kPa in 43 days, and from 20 to 40 kPa in 15 days for HRTs of 8, 4, and h, respectively (Table 5) The TMPs fluctuated at an HRT of h because the biomass concentration in the MBR was lost due to the malfunctioning water-level sensor In the last period, the TMP reached 40 kPa, and the membrane was backwashed by permeate water The need for membrane backwash after a comparatively short period operation (15 days) at a 2-h HRT was due to a high fouling speed because of a high flux (20 L/m2 per hour) This flux is slightly over the maximum allowable flux for the sponge membrane This indicates that a reduction in the HRT (increasing membrane flux) results in an increase in membrane fouling, which is in agreement with previous studies (Cho et al., 2005; KokKwang et al., 2011) In this study, the relationship between the fouling rate (kPa/day) and the HRT (h) in the sponge MBR was found to follow the power equation (dTMP/dt = 4.2474 HRT - 2.225, R2 = 0.9992) Table shows the comparison of the average fouling rates of some other reports The lowest fouling rate of 0.04 kPa/day is for the sponge MBR treating catfish pond wastewater at a flux of L/m2 per hour It indicates that the flux (and thus the HRT) strongly influences the fouling propensity of the sponge MBR The results imply that the fluxes < 10 L/m2 per hour are suitable operating conditions of the sponge MBR for treating and reuse of catfish pond wastewater If the fouling rate is slow, the membrane will be expanded, and the operation and lifetime investment for replacement and chemicals for backwashing membrane will be reduced Conclusion This study investigated the organic compounds, nitrogen, and phosphorous removal performance of a sponge MBR at HRTs of 2, 4, and h (fluxes of 20, 10, and 5, L/m2 per hour, respectively) It demonstrated that the sponge MBR exhibited the best treatment performance at an HRT of h for COD, TN, and TP removal efficiencies of 93%, 84%, and 82%, respectively The COD removal at HRTs of and h was not significantly different An HRT of 4–8 h was required to stimulate an SND process, which is important to allow for a high reduction in the TN content of the catfish farm wastewater The fouling rate was as slow as 0.04 and 0.20 kPa/day at a flux of and 10 L/m2 per hour, respectively The optimal flux for catfish farm wastewater should be in the range of 5–10 L/m2 per hour for a sponge MBR In addition, the small size, high organic and nutrient removal efficiencies, and slow fouling rate of sponge MBR make this technology a potentially attractive alternative to conventional wastewater Table Comparison of Fouling Rate in the Sponge-Membrane Bioreactor to Other Systems System a Wastewater MBR (20% sponge) Catfish pond MBR (15% sponge) MBR MABR MBR (10% sponge) MBR with MPE50 Mixed sponge MBR MBR (Mitsubishi Rayon) Synthetic Synthetic Synthetic Bathing TMP increase [kPa (days)] Fouling rate (kPa/day) Flux (L/m2 per hour) 2.5 kPa (58 days) 12 kPa (43 days) 20 kPa (15 days) 35 kPa (200 days) kPa (20 days) kPa (20 days) 45 kPa (7 days) 18 kPa (7 days) 10.5 kPa (8 days) 29 kPa (90 days) 0.04 0.20 0.89 0.17 0.40 0.30 6.43 2.57 1.31 0.32 10 20 8.75 — — — 30 30 15 a Sponge percentages are % (v/v) MBR, membrane bioreactor; TMP, transmembrane pressure References This study Jamal Khan et al (2011) Guo et al (2008b) Ngo et al (2008) Guo et al (2008a) SPONGE-MEMBRANE BIOREACTOR TREATING CATFISH FARM WASTEWATER treatment methods The treated wastewater can be recycled directly to the catfish pond during the culture period Thus, it is clear that sponge MBR technology could contribute to a more environmentally sustainable development of catfish farming in the Mekong delta, Vietnam Acknowledgments The authors would like to thank the Swedish International Cooperation Agency, the Partner Driver Cooperation Project on Sustainable Management of Ecosystem Services, for long term aquaculture production in the Mekong Delta, and the Ho Chi Minh City University of Technology for financial support for this study Author Disclosure Statement No competing financial interests exist References Anh, P.T., Kroeze, C., Bush, S.R., and Mol, A.P.J (2010) Water pollution by Pangasius production in the Mekong Delta— Vietnam: Causes and options for control Aquac Res 42, 108 American Public Health Association (APHA) (1998) Standard Methods for the Examination of Water and Wastewater, 20th ed Washington, DC: APHA Chae, K.J., Yim, S.K., and Choi, K.H (2004) Application of a sponge media (BioCube) process for upgrading and expansion of existing caprolactam wastewater treatment plant for nitrogen removal Water Sci Tech 50, 163 Cho, J., Song, K.G., Lee, S.H., and Anh, K.H (2005) Sequencing anoxic/anaerobic membrane bioreactor (SAM) pilot plant for advanced wastewater treatment Desalination 178, 219 Coˆte´, P., Buisson, H., Pound, C., and Arakaki, G (1997) Immersed membrane activated sludge for the reuse of municipal wastewater Desalination 113, 189 Guo, J., Xia, S., Wang, R.C., and Zhao, J (2008a) Study on membrane fouling of submerged membrane bioreactor in treating bathing wastewater Environ Sci 20, 1158 Guo, W., Ngo, H.H., Dharmawan, F., and Palmer, C.G (2010) Roles of polyurethane foam in aerobic moving and fixed bed bioreactors Bioresour Technol 101, 1435 Guo, W., Ngo, H.H., Palmer, C.G., Xing, W., Hu, A.Y.J., and Listowski, A (2009) Roles of sponge sizes and membrane types in a single stage sponge-submerged membrane bioreactor for improving nutrient removal from wastewater for reuse Desalination 249, 672 Guo, W.S., Vigneswaran, S., Ngo, H.H., Kandasamy, J., and Yoon, S (2008b) The role of a membrane performance enhancer in a membrane bioreactor: A comparison with other submerged membrane hybrid systems Desalination 231, 305 Jamal Khan, S., Shazia, I., Sadaf, J., Visvanathan, C., and Jegatheesan, V (2011) Performance of suspended and sponge MBR systems in treating high strength synthetic wastewater Bioresour Technol 102, 5331 199 Kok-Kwang, N., Cheng-Fang, L., Sri, C.P., Pui-Kwan, A.H., and Ping-Yi, Y (2011) Reduced membrane fouling in a novel bioentrapped membrane reactor for treatment of food and beverage processing wastewater Water Res 45, 4269 Konnerup, D., Trang, N.T.D., and Brix, H (2011) Treatment of fish pond water by recirculating horizontal and vertical flow constructed wetlands in the tropics Aquaculture 313, 57 Leiknes, T., and Ødegaard, H (2001) The development of a biofilm membrane bioreactor Desalination 202, 135 Liu, Y.X., Yang, T.O., Yuan, D.X., and Wu, X.Y (2010) Study of municipal wastewater treatment with oyster shell as biological aerated filter medium Desalination 254, 149 Metcalf & Eddy, Inc (2003) Wastewater Engineering: Treatment and Reuse, 4th ed Singapore: McGraw-Hill, Inc Ngo, H.H., Guo, W., and Xing, W (2008) Evaluation of a novel sponge-submerged membrane bioreactor (SSMBR) for sustainable water reclamation Bioresour Technol 99, 2429 Ngo, H.H., Nguyen, M.C., Sangvikar, N.G., Hoang, T.T.L., and Guo, W.S (2006) Simple approaches towards a design of an attached-growth sponge bioreactor (AGSB) for wastewater treatment and reuse Water Sci Tech 54, 191 Nguyen, T.T., Ngo, H.H., Guo, W., Johnston, A., and Listowski, A (2010) Effects of sponge size and type on the performance of an up-flow sponge bioreactor in primary treated sewage effluent treatment Bioresour Technol 101, 1416 QCVN 08:2008/BTNMT Vietnam national technical regulation for surface water quality Available at: http://vea.gov.vn/vn/ vanbanphapquy/tcmt/Pages/default.aspx QCVN 11:2008/BTNMT Vietnam national technical regulation on the effluent of aquatic products processing industry Available at: http://vea.gov.vn/vn/vanbanphapquy/tcmt/ Pages/default.aspx Sombatsompop, K., Visvanathan, C., and Ben Aim, R (2006) Evaluation of biofouling phenomenon in suspended and attached growth membrane bioreactor systems Desalination 201, 138 Soto, D., Aguilar-Manjarrez, J., and Hishamunda, N (2008) Building an ecosystem approach to aquaculture FAO/Universitat de les Illes Balears Expert Workshop May 7–11, 2007, Palma de Mallorca, Spain FAO Fisheries and Aquaculture Proceedings No 14 Rome, FAO, 2008, p 221 Thanh, B.X., Dan, N.P., and Binh, N.T (2012) Fouling mitigation in submerged membrane bioreactor treating dyeing and textile wastewater Desalination Water Treat 47, 150 U.S Environmental Protection Agency (USEPA) (2004) Guidelines for Water Reuse, U.S Environmental Protection Agency, Municipal Support Division, Office of Wastewater Management Washington, DC, No 625/R-04/108 Visvanathan, C., Benaim, R., and Parameshwaran, K (2000) Membrane separation bioreactor for wastewater treatment Crit Rev Environ Sci Tech 30, Yang, S., Yang, F., Fu, Z., and Lei, R (2009) Comparison between a moving bed membrane bioreactor and a conventional membrane bioreactor on organic carbon and nitrogen removal Bioresour Technol 100, 2369 ... Characteristics of catfish pond wastewater are mainly ammonia (NH3) with its derivatives, NH4+ -N, NO2- -N, and NO3- -N Ammonia and nitrite are harmful substances for aquatic animals In a catfish pond, ammonia... technology a potentially attractive alternative to conventional wastewater Table Comparison of Fouling Rate in the Sponge-Membrane Bioreactor to Other Systems System a Wastewater MBR (20% sponge) Catfish... Vietnam national technical regulation for surface water quality Available at: http://vea.gov.vn/vn/ vanbanphapquy/tcmt/Pages/default.aspx QCVN 11:2008/BTNMT Vietnam national technical regulation on

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